Forent Energy Ltd. drilled three wells on the Twining field during the second quarter. During the third quarter the wells were completed and tied-in for production. Field optimization efforts were conducted on the new 05-26 well to seal off a lower interval that was producing excess water, resulting in significantly decreased water production and associated handling costs.
In the Provost area, Forent's oil production was restricted in the third quarter due to a failing water disposal pump. The pump has subsequently been replaced, resulting in a 20% increase in water disposal capacity.